The sticker number under the seat has been worn off. The engine is 1988. I found a group of drawings which match the machine all from 1987. They match except for one belt which is a problem.
The blades are always engaged. When the deck is disengaged the belt does not go slack enough to let the belt slip on the drive pulley. There is no tensioner pulley. What I think happens is the engagement level lowers the deck and at the same time moves the deck back slightly which is probably how the belt gets tensioned. It may be working properly but the belt on there may be too tight.
The belt on all the drawings of machines similar all have a deck drive belt of 754-0280. The MTD site lists that belt at ½ x 53 ½ inches. That size would never work on this machine. The belt on there is 754-0329 listed as .625 x 69.28. Some non-MTD sites list the 754-0280 as .700 x 53.17 which also never work. The belt on there measures about 70 inches, is too tight and not the right part number, it’s754-0329. ??
I’d like to get a belt that works but that will probably have to be done by trial and error. It makes starting the thing harder because of the blades being engaged.
The compression is 30psi and way to low even with compression release. I think your right Friiy, that something is going on with the valves. It could also be a sheared key and the flywheel only slightly off but most likely valves. With the air filter off there seems to be a slight mist in the throat which much be caused by the intake valve leaking.
Bill_H,
The sticker under the seat has AirCap Industries on it but the rest is worn off. Given the 1986 and the drawing match to MTD it’s MTD made.
Not a bad rig for $100 and it came with the double cloth bags and blower hose. The guy had the solenoid wired to the ground post of the ignition switch for some reason. He ran a separate wire to do that. The original wire was inplace but unconnected. ??
Friiy, you mentioned these carbs were weird. It has a 4 inch tube with small holes you can unscrew and remove from the top of the carb which was partly plugged. Never saw such a tube before. Clearing that made it start and run a bit better.